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[JS Required] Boeing’s Inadequate ‘Training, Guidance and Oversight’ Led to Mid-Exit Door Plug Blowout on Passenger Jet

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  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    It's time for Boeing to end.
    It's a hazardous organization. The more they get away with, the more they are going to cut corners.

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    All Boeing needs to make this problem go away is a modest investment in $TRUMP....

  • It's time for Boeing to end.
    It's a hazardous organization. The more they get away with, the more they are going to cut corners.

    "They're too big to fail, they're the only major domestic aircraft manufacturer!" Ok so nationalize them

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane

    Something about the phrasing giving agency to the door plug is hilarious to me. The plug said “im out, see ya”

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    And all that inadequate training, guidance and oversight was due to priorising profits over safety.

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    But no third-party js.

  • ​FAA cited for ineffective oversight of Boeing’s known recordkeeping issues

    WASHINGTON (June 24, 2025) — The National Transportation Safety Board Tuesday said the probable cause of last year’s in-flight mid-exit door (MED) plug blowout on a Boeing 737 MAX 9 was Boeing’s failure to “provide adequate training, guidance and oversight” to its factory workers.

    The NTSB also found the Federal Aviation Administration was ineffective in ensuring Boeing addressed “repetitive and systemic” nonconformance issues associated with its parts removal process.

    The NTSB also concluded that in the two years before the accident, Boeing’s voluntary safety management system, or SMS, was inadequate, lacked formal FAA oversight, and did not proactively identify and mitigate risks. The investigation found that accurate and ongoing data about overall safety culture is necessary for an SMS to be successfully integrated into a quality management system.

    On Jan. 5, 2024, the Boeing 737-9, operated as Alaska Airlines flight 1282, was climbing through 14,830 feet about six minutes after takeoff from Portland, Oregon, when the left MED plug departed the airplane. During the rapid depressurization, some passengers’ belongings were sucked out of the airplane, oxygen masks dropped from the overhead passenger service units, and the door to the flight deck swung open, injuring a flight attendant. In addition to the flight attendant, seven passengers received minor injuries. The two pilots, the other three flight attendants and the remaining 164 passengers were uninjured. The flight was destined for Ontario, California.

    “The safety deficiencies that led to this accident should have been evident to Boeing and to the FAA — should have been preventable,” NTSB Chairwoman Jennifer Homendy said. “This time, it was missing bolts securing the MED plug. But the same safety deficiencies that led to this accident could just as easily have led to other manufacturing quality escapes and, perhaps, other accidents.”

    The MED plug was found in a Portland neighborhood two days after the accident. When investigators examined the recovered plug, they found evidence that the four bolts needed to secure the plug were missing before the accident occurred. Without the bolts, NTSB investigators found the unsecured plug “had moved incrementally upward during previous flight cycles” until it departed the airplane during the accident flight.

    The airplane had been delivered to Alaska Airlines three months earlier. Investigators determined that the door plug was opened without the required documentation in Boeing’s Renton, Washington, factory on Sept. 18, 2023, to perform rivet repair work on the fuselage. The door plug was closed the following day. While Boeing’s procedures called for specific technicians to open or close MED plugs, none of the specialized workers were working at the time the door plug was closed. The absence of proper documentation of the door plug work meant no quality assurance inspection of the plug closure occurred.

    The investigation also highlighted the need for additional training on flight crew oxygen masks and their communication systems and the need for greater voluntary use of child restraint systems by caregivers of those under two years of age.

    The NTSB issued new safety recommendations to the FAA and Boeing. Previously issued recommendations were reiterated to the FAA, Airlines for America, the National Air Carrier Association and Regional Airline Association.

    The executive summary of the report, including the findings, probable cause and safety recommendations, is available online​. Additional material, including the preliminary report, previously issued safety recommendations, news releases, the public docket, investigative updates and links to photos and videos, is available on the accident investigation webpage.

    The final report will be published in the coming weeks on NTSB.gov.

    That they didn't have enough technicians trained in this to be able to ensure that one was always available during working hours, or at least when it was glaringly obvious that one was going to be needed that day, is . . . both extremely and obviously stupid, and par for the course for a corp whose sole purpose is maximizing profit for the next quarter.

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    P
    Seems more like someone got confused and dumped info for chicken pox instead of “chicken pops”
  • 84 Stimmen
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    iavicenna@lemmy.worldI
    Oh nice I hope they end up destroying themselves
  • 74 Stimmen
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    O
    The point is not visuals, though I know what you mean. The point is to gain the introspection and Brain chemistry changes. Micro dosing less than . 5 grams daily for short periods NOT LONGTERM, are very effective control vs SSRIs. Large mega doses are where the real changes happen. I highly recommend significant research and carrful planning if you choose this route. Safety. Trip sitters. Be safe. There has been major changes in PTSD war veterans and all sorts if mental health issues.
  • Russian Lawmakers Authorize Creation Of National Messaging Service

    Technology technology
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    1
    34 Stimmen
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    C
    Are there substantial numbers of Russians who seriously wouldn't be wise to this?
  • 1 Stimmen
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    A
    If you're a developer, a startup founder, or part of a small team, you've poured countless hours into building your web application. You've perfected the UI, optimized the database, and shipped features your users love. But in the rush to build and deploy, a critical question often gets deferred: is your application secure? For many, the answer is a nervous "I hope so." The reality is that without a proper defense, your application is exposed to a barrage of automated attacks hitting the web every second. Threats like SQL Injection, Cross-Site Scripting (XSS), and Remote Code Execution are not just reserved for large enterprises; they are constant dangers for any application with a public IP address. The Security Barrier: When Cost and Complexity Get in the Way The standard recommendation is to place a Web Application Firewall (WAF) in front of your application. A WAF acts as a protective shield, inspecting incoming traffic and filtering out malicious requests before they can do any damage. It’s a foundational piece of modern web security. So, why doesn't everyone have one? Historically, robust WAFs have been complex and expensive. They required significant budgets, specialized knowledge to configure, and ongoing maintenance, putting them out of reach for students, solo developers, non-profits, and early-stage startups. This has created a dangerous security divide, leaving the most innovative and resource-constrained projects the most vulnerable. But that is changing. Democratizing Security: The Power of a Community WAF Security should be a right, not a privilege. Recognizing this, the landscape is shifting towards more accessible, community-driven tools. The goal is to provide powerful, enterprise-grade protection to everyone, for free. This is the principle behind the HaltDos Community WAF. It's a no-cost, perpetually free Web Application Firewall designed specifically for the community that has been underserved for too long. It’s not a stripped-down trial version; it’s a powerful security tool designed to give you immediate and effective protection against the OWASP Top 10 and other critical web threats. What Can You Actually Do with It? With a community WAF, you can deploy a security layer in minutes that: Blocks Malicious Payloads: Get instant, out-of-the-box protection against common attack patterns like SQLi, XSS, RCE, and more. Stops Bad Bots: Prevent malicious bots from scraping your content, attempting credential stuffing, or spamming your forms. Gives You Visibility: A real-time dashboard shows you exactly who is trying to attack your application and what methods they are using, providing invaluable security intelligence. Allows Customization: You can add your own custom security rules to tailor the protection specifically to your application's logic and technology stack. The best part? It can be deployed virtually anywhere—on-premises, in a private cloud, or with any major cloud provider like AWS, Azure, or Google Cloud. Get Started in Minutes You don't need to be a security guru to use it. The setup is straightforward, and the value is immediate. Protecting the project, you've worked so hard on is no longer a question of budget. Download: Get the free Community WAF from the HaltDos site. Deploy: Follow the simple instructions to set it up with your web server (it’s compatible with Nginx, Apache, and others). Secure: Watch the dashboard as it begins to inspect your traffic and block threats in real-time. Security is a journey, but it must start somewhere. For developers, startups, and anyone running a web application on a tight budget, a community WAF is the perfect first step. It's powerful, it's easy, and it's completely free.
  • 386 Stimmen
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    Melon Usk doomed their FSD efforts from the start with his dunning-kruger-brain take of "humans drive just using their eyes, so cars shouldn't need any sensors besides cameras." Considering how many excellent engineers there are (or were, at least) at his companies, it's kind of fascinating how "stupid at the top" is just as bad, if not worse, than "stupid all the way down."
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    L
    Okay, I'd be interested to hear what you think is wrong with this, because I'm pretty sure it's more or less correct. Some sources for you to help you understand these concepts a bit better: What DLSS is and how it works as a starter: https://en.wikipedia.org/wiki/Deep_Learning_Super_Sampling Issues with modern "optimization", including DLSS: https://www.youtube.com/watch?v=lJu_DgCHfx4 TAA comparisons (yes, biased, but accurate): https://old.reddit.com/r/FuckTAA/comments/1e7ozv0/rfucktaa_resource/
  • 3 Stimmen
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    M
    Are most people in "the west" worse off today than they were 150 years ago? Are there fewer well functioning democracies than there were then? Has no minority group seen any improvement in their freedom? Has there been no improvement in how people interact with each other? No improvement in poverty?